Page Last Updated: 15 MAY 2013
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Documents Issued within the last 90 days will be posted below; such as, Service Bulletins, Technical Bulletins, Service Letters and Temporary Revisions.
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Model 900 Helicopters- Bulletins & Letters
| Size | Publication Number | Publication Title | Issue /Reissue Date |
160K |
TB900-043 | MODIFICATION OF THE NACA INLET DOOR PANEL ASSEMBLY Procedures in this Bulletin give owners and operators information to modify the NACA inlet door panel assembly with a toggle switch that has a detent which will lock the OVERRIDE (CLOSED) switch position for the closed inlet door to make sure the switch cannot be accidentally put in the NORMAL (OPEN) position. |
08 APR 2013 |
334K |
SL900-078 | INSPECTION OF GOODRICH HOIST MOTORS This letter tells owners and operators to do an inspection of the rescue hoist motors shown in the attached Goodrich Alert Service Bulletin 44301-10-15 (ref. EASA EAD 2013-0077-E and FAA EAD 2013-06-51) |
26 MAR 2013 |
74K |
TB900-044 | INCREASE OF OPERATIONAL WEIGHT LIMIT TO 6770 LB (3070.82 KG) Procedures in this Bulletin give owners and operators information to increase the operational weight limit of MD Explorer rotorcraft with PW207E turbine engines installed. |
15 MAR 2013 |
Model 369D,E,FF, 500N, 600N Helicopters - Bulletins & Letters
| Size |
3 6 9 D |
3 6 9 E |
3 6 9 FF |
5 2 0 N |
6 0 0 N |
Doc. # | Title | Issue /Reissue Date |
| 329K |
X | X | X | X | TB369E-005, TB369F-008, TB500N-005, TB600N-010 |
SLANT CONSOLE INSTALLATION Procedures in this Bulletin give owners and operators information to modify existing rotorcraft for installation of a slant console. |
15 MAY 2013 | |
| 148K |
X | X | SB369E-108 SB369F-094 |
AFT POSITION AND ANTI-COLLISION LIGHT MOUNTING INSPECTION, REPLACEMENT AND REPAIR
The aft position light mounting bracket assembly is experiencing fatigue cracking due to increased weight of LED position light. Procedures in this Bulletin give owners and operators information to replace the aft position light mounting bracket assembly and inspect and repair the anti-collision light support assembly. |
14 MAY 2013 | |||
| 101K |
X | X | X | X | SB369D-206R1 SB369E-101 R1 SB369F-086 R1 SB500N-043 R1 |
INSPECTION OF P/N 369D292028, AFT PASSENGER STEP ASSEMBLIES, ON EXTENDED LANDING GEAR ASSEMBLIES Examine aft passenger step assemblies for possible cracked welds. This bulletin gives instructions for a three-part inspection: Initial visual inspection with 10X magnification Proof-load test with visual inspection Fluorescent penetrant inspection of the aft passenger step assembly welds |
26 APR 2013 | |
| 208K |
X | X | X | X | X | SB369D-211R1 SB369E-106 R1 SB369F-092 R1 SB500N-048 R1 SB600N-056R1 |
UPPER MAIN ROTOR PITCH CONTROL ROD END, PN 369A1011 INSPECTION AND REPLACEMENT MDHI has determined that upper main rotor pitch control rod ends, PN 369A1011, identified with vendor code 5963 and a manufacture date between 07-01-11 and 08-31-11, installed on aircraft or purchased as spares between July 2011 and November 2012 can show a breakout torque that is too high after an unusually short time. |
16 APR 2013 |
Model 369H Helicopters - Bulletins & Letters
| Size | Doc. # | Title | Issue /Reissue Date |
| 208K |
SB369H-253r1 |
UPPER MAIN ROTOR PITCH CONTROL ROD END, PN 369A1011 INSPECTION AND REPLACEMENT MDHI has determined that upper main rotor pitch control rod ends, PN 369A1011, identified with vendor code 5963 and a manufacture date between 07-01-11 and 08-31-11, installed on aircraft or purchased as spares between July 2011 and November 2012 can show a breakout torque that is too high after an unusually short time. | 16 APR 2013 |